DEEPCLEAN Additive Effectively Cleans Deepwater Well Shut-in for 10 Years

Published: 01/01/2010

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Well Information

 
Location Mississippi Canyon, Gulf of Mexico
Completion Date Nov. 29, 2009
Interval completed TD at 12,331 ft MD (3758 m)
Hole volume annulus – 2,500 bbl, work string – 189 bbl
Displacement type Indirect

The Situation

A Gulf of Mexico operator planned to re-enter a well that had been shut in for at least 10 years with 10.5 lb/gal (1.2 sg) synthetic based mud. The operation would require drilling a sidetrack before attempting to complete the well. Owing to the unknown condition of both the mud and casing, the operator required an additive that offered the best possible efficiency for cleaning and water wetting the casing.

The Solution

The operator selected a wash spacer formulation incorporating the new dual purpose DEEPCLEAN product, which also was specified as an additive in the transition spacer. The DEEPCLEAN product is engineered for thorough and efficient cleaning of technically demanding well cleanups. DEEPCLEAN product was especially designed and tested to outperform other cleaning products even in laminar flow. In addition, the displacement was designed using M-I SWACO best practice design techniques. e well. Owing to the unknown condition of both the mud and casing, the operator required an additive that offered the best possible efficiency for cleaning and water wetting the casing.

The Results

After circulating only 200 bbl of seawater, the NTU reading was less than 100, indicating a successful casing cleanup and displacement. Further evidence of a successful cleanup was observed when the well was displaced with the clear brine and the final NTU reading was reduced to 25 with only a trace of solids.

The Details

The spacers were mixed on the rig with the following formulation:

DEEPCLEAN Additive Effectively Cleans Deepwater Well Shut-in for 10 Years

After the spacers were mixed, they were pumped in the prescribed sequence into the work string. Upon arrival of the transition spacer at the surface in the annulus, the pumps were stopped while the crew cleaned out the gumbo box and shakers. This was an unfavorable situation as it resulted in the spacers being static in the riser annulus for 2 hr, which potentially can lead to solids falling back into the wellbore and degradation of the spacers. After 200 bbl of seawater were circulated behind the spacers, the NTU reading indicated the hole was clean. Subsequent cleanup tools were POOH with no evidence of residual mud left in the hole. Further, all of the downhole equipment deployed after the displacement showed no indicators of problems associated with mud residue.

“The DEEPCLEAN*product proved to be highly efficient at cleaning a challenging deepwater well, despite less-than-ideal pumping conditions. Thus, the operator was able to successfully re-enter a well shut-in for 10 years.”John Carboni, Project Engineer, M-I SWACO

Questions? We’ll be glad to answer them.

If you’d like to know more about the DEEPCLEAN product and how it’s performing for our other customers, please call the M-I SWACO office nearest you.

Location
Gulf of Mexico, United States, North America, Offshore
Details

Challenge: A Gulf of Mexico operator planned to re-enter a well that had been shut in for at least 10 years with 10.5 lb/gal (1.2 sg) synthetic based mud. The operation would require drilling a sidetrack before attempting to complete the well. Owing to the unknown condition of both the mud and casing, the operator required an additive that offered the best possible efficiency for cleaning and water wetting the casing

Solution: The operator selected a wash spacer formulation incorporating the new dual purpose DEEPCLEAN product, which also was specified as an additive in the transition spacer

Results: After circulating only 200 bbl of seawater, the NTU reading was less than 100, indicating a successful casing cleanup and displacement. Further evidence of a successful cleanup was observed when the well was displaced with the clear brine and the final NTU reading was reduced to 25 with only a trace of solids

Products Used